updated 16 june 2022
(Shown below: modified 1965 oil pump on 1965 engine, installed in my 1960 Rambler American Super wagon.)
The lubrication system in this engine has proven to be adequate to the task. This engine was designed before the Interstate highway system existed; it was not intended for extended high-speed operation but seems to be just fine with all components in good order.
Lubricants are so good today that any good quality 10W-30 or 10W-40 is more than adequate. Today (Nov 2021) I run O'Reilly Auto Parts house brand 10W-40. On a recent 2500 mile Southwest road trip from sea-level through 7000 feet, peak oil temperature did not exceed 230 F, average was about 200 F. If you plan on sustained operation above 3000 RPM, I suggest at minimum measuring sump temperature and backing off on excessive temperature rise. Hot oil is thin oil. I have found that a substantial oil cooling system is required for hard use about 3200 rpm.
My recommended oil change interval is 2000 miles, or less after hard use (my roadster). 2000 miles is not excessive. These are old engines, there is a lot of ring blowby and the crankcase is not sealed. Also I refer to this experience as the most convincing argument, and this experience was on the modern 199ci engine, not this old thing. Oil's cheaper than engines.
My personal assessment of "the zinc issue" is that it may possibly be needed during engine break-in, and you should be excessively kind to a new, expensive motor anyway. If it's not needed, no harm done. Once broken in it appears that Zn and P (in ZDDP or ZDTP form) is just not necessary.
The oil pump is an externally mounted gear pump. The pump inserts into the lower side of the block, pulls oil from the pan and pushes directly into the main gallery. Top end (rocker shaft, etc) is lubricated by an external line that carries oil from a tap on the block up to the head casting where it flows upward through a rocker shaft support, into the hollow shaft and from there to each rocker. On earlier engines the top-end source is the main gallery, eg. full engine oil supply. On later engines the top end is fed by an intermittent source generated by a flat on the camshaft's front journal that pulses the main gallery feed, to limit oil flow to the top end.
The oil pump can be removed fairly easily. Remove one of the two bolts attatching the idler arm to the chassis, loosen the other, and swing the idler arm out of the way. The pump will come out and just clear everything. On my modified pump I take the hose off, leaving the 90-degree elbow in place.
Crankshaft main journals are fed directly from the main gallery as is each cam bearing. Connecting rod bearings receive oil via drilled crank. The connecting rod big end has a squirt hole that lubricates the cam lobe journals (but there are conn rods with two, or no, holes, both flathead and OHV, so who really knows). The cam is also splash lubricated. Some years have piston squirt lubrication via conn rod squirt hole.
There are at least three different oil pumps that fit in this engine, with caveats:
Most discussion and photos on this page and this site are of the most common M61 pump unless specified otherwise.
The Melling M61 fits all 195.6 engines before 1965. Oil filtration is elsewhere, and an afterthought, indeed, an option at time of purchase. You want a filter. Though a "bypass" system it does adequately filter the oil over time. engine has no provision for in-block pressure relief.
For many years, and in two engines, I have run a stock M61 pump with fabricated cover for external filtration. See below for details.
1965 has it's own, superior, pump with full-flow filtration. The 1964/1965 pump fits only into 1964/1965 blocks. It cannot be used on earlier engines. The advantages of the 1964/1965 full-flow pump are obvious -- full-flow filtration. For use in the early American chassis (1958..1963) the pump must be installed before the engine is installed in the chassis. (The M-61 pump can be removed/installed on the engine with the engine in the car.) The limiting feature is that the three bolts attaching pump to block need to be fully removed inr order to slide the cover off the pump body, which makes room for the pump body to come sufficiently far out of the block.) I previously had written that 'attached filter assembly cannot be used', but it can be done, with the non-removal caveat above. Another solution I have used is to modify the the pump body to accept 3/8" NPT to AN flare fittings to connect a remote oil filter. This is very straightforward and works great. It also provides a provision for oil cooling, if needed.
The 1964/1965 block has no provision for an oil pressure relief. The 1964/1965 pump has over-pressure relief incorporated into the pump cover.
The E-Stick pump was used in E-Stick-optioned cars for only 18 months, 1962 to 1963 I think. It was a disaster product-wise, an automatic clutch operated by engine oil pressure. The pump body and gears are probably 50 &percent; larger and correspondingly higher-volume than the M61. However the cover for this pump contained E-Stick "logic" and solenoids, and requires a fabricated cover for use as a "hot rod" pump for non-E-Stick cars. The M61 cover is too small.
An E-Stick pump with fabricated cover is now installed in my roadster's endurance motor. In that engine I run 15W-50 oil and when cold, oil pressure at 1200 RPM is over 75 PSI, so the engine must be warmed up to at least 125 F before use. With thinner oil this would likely be less of a problem.
The E-stick pump chamber bores are 1.615" diameter and 1.49" deep, vs 1.355" bore and 1.40" deep for the M61.
Vaseline packing.
oil into center gallery plug.
Here are some photos of a dirty 1965 block. Somewhere I have the photos of this engine clean, and another, earlier engine for comparison. I'll put them up eventually. (This 1965 engine is now running in my 1960 American wagon.)
The factory service manual mentions this, but here is a photo: the 1964, 1965 block has that visible extra top-end-oil port at the front side of the block, and the front cam bearing has two holes to accommodate it. The front cam journal has a flat (chopped off on a chord) so that the missing cam journal connects the two ports, for a metered squirt of oil instead of a continuous flow as in earlier engines.
You can mix'n'match cams and bearings if needed, but keep in mind that if you do not have all components -- two-hole bearing, slotted front camshaft -- the top end will receive no lubrication! In which case simply plumb the oil from the main gallery, an inch below, as per older cars. (I'm running full-flow in my roadster engine with no downside).
Oil pumps don't get a lot of attention when motors are built or refreshed. However they are a component critical for durability and at this great age used pumps must be inspected closely -- mainly for gear-to-body clearance.
Oil volume and pressure is dependent on wear in the pump. Gear pumps run close metal-to-metal tolerances to push liquid; they are very sensitive to clearance due to wear. Unfortunately we do not have a specification for gear-to-body clearance but I have recorded clearances from four pumps; one new-manufacture old-stock replacement ("NEW"), an old-stock "remanufactured" replacement ("REMAN"), and here, a used 1965 pump modified for use in a 1960 American ("65MOD"), assembled from selected used parts; and an E-Stick pump put together from NOS parts. The 1965 pump, from a low-milesage engine, received mix'n'match best-of-the-pile gears.
AMC oil pump clearance measurements | |
Pump ID | Gear to body clearance |
---|---|
NEW | .003" |
REMAN | .006" |
65MOD | .003" |
ESTICK | .003" |
New-manufacture old stock M61 pump.
Remanufactured (rebuilt) old stock M61 pump.
Modified 1965 pump. Used body and mix'n'match gears.
Unfortunately it is not enough to rely on clearance alone. The part of the pump most subject to neglect -- infrequent oil changes, crappy oil -- are the outer edges of the gear teeth that sweep oil around the pump cavity. Grit in the oil that approaches the gear to pump clearance wears away the body and gear teeth. The teeth edge become chipped and rough from pumping grit suspended in the oil. The feeler gauge senses the peaks of the teeth -- and misses the rough valleys caused by wear.
Gear teeth need to be examined closely for corrosion (from sitting unused in storage) and for pitting at the edge. The easiest way to see pitting is to hold a known straight edge (quality rule such as a 6-inch Starrett, or a new unused single edge razorblade) to the gear edge and view it with a strong backlight.
A new gear will show extremely fine, even and regular machined surface. A worn gear will be rough and pitted.
The photos below show wear on old gears, and what a new gear looks like, taken from the new-manufacture pump shown above. The backlit photos aren't very good; it takes two hands to do right, here they're propped up on a Starrett ruler and backlit with a small light. Better to hold in two hands up to the sun.
These are new replacement gears, unscored and edges straight.
Oil volume and pressure increases with engine RPM since the pump is geared to the camshaft. Additionally, when oil is cold it is thick. For these reasons there is an oil pump ressure relief valve, a plunger and a spring. Excess oil pressure lifts the plunger off it's seat, dumping main gallery oil into the sump. Simple. On all 195.6's through 1963, the spring and plunger are under a plug screwed into the block outside, aft of the oil pump. In 1964 and 1965, oil pressure relief plug, spring, plunger are in the oil pump cover.
The spring in the 1964/1965 pump is a different length (shorter) than the in-block spring.
The oil pump and relief valve specification is 55 to 60 PSI at 2200 rpm (per 1962 TSM).
Here is more information than you ever wanted to know about this spring. It features a little more heavily into this story further below.
AMC oil pump pressure relief valve spring, part 3112400, Jones design 21519-0 | |
length | 2-5/8" |
diameter | 7/16" |
wire diameter | 0.057" |
turns | 22.3 |
This is not authoritative, measuring the longest used spring I have from a 1965 engine that showed little wear; it is installed and in use and fully warm engine 2500 rpm, oil pressure was above 55 psi.
1965 only AMC oil pump pressure relief valve spring, part xxx | |
length | at least 2.35" |
diameter | 7/16" |
wire diameter | 0.057" |
turns | 21 |
The valve cover design is pretty good but engine oil flows along the rocker shaft and pours steadily right onto the spot where the cover gasket meets the head, and they often develop a minor seep there, even with a new gasket. any tendency to leak is made worse by the oil pouring off the rocker shaft onto the seal.
A simple twist of steel wire around the far end of the rocker shaft provides a path for oil to return to the cavity in the head casting. there is now no oil leak or mess even when running with the valve cover off. the same wire twist has been in place for nine years. it is tight enough to have a shape, but loose enough that it can't wedge itself between the rocker and washer. Even if it wears into two pieces they'll lay harmlessly on top of the head. here's a brief movie (AVI format) of it in operation.
The bypass oil filtration system on at least the earlier models was an extra-cost option. Many 195.6's have no oil filtration at all. If your engine does not have a filter (mounted adjacent to the radiator, it's fairly obvious) you should find one and install it. It's quit easy to do.
I originally assumed without doing research that the bypass filtration system was inadequate, and engineerd a full-flow system, below. An AMC forum member's research found that given in operation the volume of oil is such that all of the oil is passed through the filter in a surprisingly short period of time. Full-flow filtration is preferable (a given particle will be stopped the first time through the pump) but given adequate oil changes and today's high quality oil, is not a reason to worry.
So my original impetus for working out full-flow filtration wasn't as critical as I'd imagined, but full-flow filtration made oil cooling possible.
it's .009" thick, hard paper. it's photographed here on 1" grid paper, 10 lines per inch.
I modified the M61 pump for full-flow filtration by fabricating a new pump top cover with pressurized oil outlet and fabricating a steel gasket that blocked the pump's main gallery output. With this modification oil is pumped out the cover, through a 90-degree 8AN line (for chassis clearance) to the cooler and filter, then into the main gallery. details follow.
below are photos of the original 2010 installation. the rubber hose/nipple system shown here was swapped out long ago for proper stainless steel braided, PTFE lined, crimped 6-AN fittings a few months after these photos were taken. These photos however show component location well. The oil filter mount is from a remote oil filter kit. It's mounted via bracket bolted to the timing chain cover bolts.
The pump (green assembly with three cover bolts, lower left in the first picture) sucks oil from the pan and as modified, pushes oil out the cover through the lower hose. Oil flows through cooler, filter then into the center of the main gallery where the AMC factory conveniently put a 1/4" NPT tapped hole, directly above the original pump feed location.
Sadly I don't have a single photo of the steel shim "gasket" that blocks the pump-to-gallery outlet, but it was easy to fabricate -- I simply traced out the oil pump base gasket onto .025" sheet steel and drilled all of the holes except pump outlet.
The new pump top has an outlet directly opposite the original outlet in the pump body; oil under pressure now exits up not down. The cover is fabricated from two pieces of 1/4" steel stock, the small piece stiffens and builds up height for sufficient threads in the tapped NPT hole, and allowed the driven-gear lubrication well to be a simple through hole in the larger plate. The small milled groove feeds pump inlet oil (not outlet pressure) to the top of the driven gear and matches the factory configuration.
The location of the outlet hole was fairly touchy; note that it is not centered in the gear output cavity, but slightly to one side. This is due to interference with the top pump bolt. socket-head bolts are required. The hole seems large but the effective diameter is actually the ID of the fitting, about 3/8".
After welding, the plate warps; I milled it more or less flat then ground it flat flat with 80-grit wet-or-dry on a ground cast iron plate. Flatness matters here, this is the mating/sealing surface for the pump gears as well as the pump body gasket surface. The gasket is dimensionally thin, hard, and subject to full pump pressure, and this is a core mission-critical part. It's worth the extra effort to get this perfect. Note also that the gasket is trimmed around the new outlet hole.
To the cover I added a 90-degree 3/8" pipe to 1/2" flare tubing adapter. I used a stainless steel part instead of plumbing store brass. I needed to shave about 1/16" off one side of the flare adapter to clear the hex socket bolt head. I assembled the adapter and plate on the bench and was able to get it very tight. It should be left pointing towards the front of the car, up 45 degrees or so from horizontal; this gives maximum clearance under the car and allows for easy wrench access.
(a hardware store type brass 90 degree hose nipple is shown here; when i switched out the rubber hoses I installed much larger bore and higher quality stainless steel AN flare elbow.)
Note also that internally, the fitting must be flush or below cover plate flush. I removed metal from the fitting so that it was 0.010" or so below flush when assembled.
the hex head bolts shown in this early photo interefered with the line fitting; I replaced all the bolts with socket head bolts. The top bolt also needs to be 3" long rather than the stock 2.5" given the additional thickness.
This system puts full un-bypassed pump pressure into the inlet of the filter, which only matters for OEMs making millions of cars where owners do no maintenance. The stock oil pressure relief valve remains in the stock location. The filter (initially Wix 51374, now the taller Wix 51088) has both anti-drainback and a 10 psi internal bypass. The filter is mounted upside down so the anti-drainback feature isn't needed.
Here is my roadster with above oil pump mods, and the addition of an Accusump system to deal with oil pressure loss in hard turns (certainly not needed in a street car).
The critical hoses that appear to stick up exposed are carefully placed to fit into recesses in the hood and aren't as exposed to harm as the appear to be here. It's tight in there, it's a small car.
There's a lot of hose in there, and it's "only" 8AN. Bends are all large radius, two 45-degree fittings and one 90, necessary for clearance out of the pump, but it was bored and smoothed out. Also see the smoothing and debugging done to the pump.
But this isn't a big modern V8 oiling system. here, the pump feeds the main gallery through a 5/16" hole. With the admittedly weak test of blowing through the hose, there's little restriction. by 1600 rpm the relief valve is open, limiting pressure to 60 psi, so volume is adequate for that to happen. In any case it's been running for years with good effect.
With cold 20W-50 oil pressure at idle has the relief valve open; even 2000 rpm pushes cold (60F) pressure past 75 psi, hence the switch of oils.
As of Nov 2021 this system has three years and over 35,000 miles of demanding use.
When the engine was again overhauled in 2016/2017 this modded pump had been in use for six years and some 50,000 miles. There is some minor scuffing of the cover by the gears. I neglected again to photograph the steel blocking gasket.
i did not re-use this pump body and gears; it was a used part when i
started, and I found a brand-new pump to replace it. it received the same
modifications and fabricated top cover and is now in service. gear to body
clearance is tighter too.
A friend of mine recently bought a '63 hardtop as an imcompleted project. The engine was nicely built, and the builder also modified the oiling system for full-flow filtration.
In this case the builder drilled and tapped the stock, factory cover for the 90-degree elbow. I didn't do that because I thought there would not be enough threads, but it seems adequate here. (I do have a tendency to overbuild.)
Some time after 2008 I started treating my little '63 American as a sport(y) car, and pushing the engine harder and harder. In 2010 I rebuilt it, using a local shop for the machine work, what I thought at the time was good work.
In 2016 I burned that engine up, melting all the rod big-end and main bearings in an admittedly stressful situation: 24 Hours of LeMons Hell On Wheels Rally (rally, not race); wide-open-throttle in top gear, climbing a 20% grade in Death Valley in August 2015, 115F air temperature.
I managed to limp home with an increasingly loud bearing rap. before the teardown for the current (2017) build I did some tests and experiments to determine the source of the failure. Suspecting hot oil, I inserted a Stewart Warner temperature sensor into the rear-most main gallery port (1/8" NPT) and drove up the local freeway -- within 10 miles and at modest speeds (60-ish mph) the temperature rose to nearly 230F. Now 230F is fine -- but this was a brief test drive in cool weather. Wide open throttle desert highway 115F ambient is quite another thing.
That only partially explained the low operating oil pressure. I pulled the engine out, and examined the oil pump pressure relief valve spring, and found that it had collapsed.
The failed spring was fairly easy to find; there was little tension on it when I removed it from the block. Shimming it (ultimately with a 3/8" spacer) brought oil pressure up to normal.
Conclusion: failure was caused by two factors: severe engine oil overheating and a collapsed oil pump pressure relief valve spring. Oil viscosity is directly relate to temperature, so the oil film was thin. The failed (soft) spring lowered oil pressure from it's typical 55..60 psi to 45, then 40, then 35... psi, at highway speeds.
Upon disassembly, all of the connecting rod big end bearings had melted in place. the 2017 build included a substantial oil cooler. now, under similar load conditions, oil temperature stays under 220F, and on modest highway use 190F (engine coolant temperature).
In 2017 I saved up a lot of pennies and had a professional builder, Pete Fleming in the San Fernando Valley, build my next engine. Many pennies. Nearly all of the hefty expense went into top-notch machine work, such as very careful clearancing of crank and rod bearings and journals.
Pete clearanced this engine to run 20W-50 Valvoline VR1 racing oil (available in Los Angeles). This oil is thick when cold; during warmup I keep RPMs down so that oil pressure stays under 75 psi. One cold morning spiked oil pressure high enough to poop out the oil filter gasket. Road side repair, limped home, did more research, and switched to Mobil1 15W-50, one of the few full synthetics to have sufficient zinc and phosphorous for the (highly stressed) flat tappets because it has beter viscosity index [Nov 2021 note: I now think the zinc worry on broken-in engines is a waste of time].
Here are the documents I ended up with after my oil research.
I'll allow my squirrel helper here to show you the oil cooling and filtration system installed on the roadster engine. Her right hand is on the cooler feed line. She doesn't actually accomplish much around here but ensures that no peanuts are left lying about.
The current system consists of the stock pump modified for full flow oil filtration, a fairly large stacked-plate cooler with fan, and an Accusump accumulator system from Canton Racing Products. how and why I got here is described below. The full oiling system is visible, other than the oil filter hiding beneath the alternator. The photo below shows the oil pump (red, protruding from the block), the line running to the alternator forward, and the line from the Accusump feeding the main gallery, top and center. Lines are PTFE lined stainless steel braid, crimped 8AN fittings.
Given that I had already made the full-flow filtration modifications back in 2016, adding an oil cooler was relatively easy. Oil cooling is flatly necessary for anything more than casual Sunday drives. However without the substantial mod to the oil pump described below there is no way to get at the oil flow.
For the 2017 rebuild I installed a 1/8" NPT bung for a Stewart Warner temperature sensor down low in the pan.
A note on oil cooler mounting: I originally had the oil cooler mounted down in the valance, a big screened hole below the right headlight. In Death Valley (or equiv.) this was great -- however in cool/cold weather it took over 30 minutes to warm up. It's since been moved to it's current location under the hood.
Here it is mounted on a bracket bent to fit the cooler onto the curved inner fender and to provide about an inch of clearance for air flow. I'm not totally happy with it circulating under-hood air, but it seems adequate. (If I 'hole' the inner fender the fan will then draw cooler air from the wheel well area, should I need it.)
In my installation I have a fairly elaborate all-electronic closed-loop cooling system controlling the oil cooler fan. However, the inline thermoswitch built into the cooler is more than adequate.
These modifications allow me to run this engine at more or less full output
for extended periods and have engine oil temperature stay below 200F. On a
6000 mile drive across the country (Los Angeles to the southeast, for the 2016
HOT ROD Power Tour) peak oil temperature was 220F.
Yet another serious oiling system problem appears only when the car it's in is driven hard and fast on mountain/canyon roads like we have here in California. I do planned/routed "tours" with a vintage sports car crowd and the roadster is now fast enough to cause severe loss of oil pressure in turns due to sloshing in the pan. I neglected to take the time to baffle the pan when the engine was built. the sump only holds four quarts, though I often drive with five, but then I get oil misting issues and increased oil consumption.
Someone on the 2018 California Melee suggested I look into an Accusump; after research and email discussion with Jeff at Canton Racing Products i bought and installed one.
Briefly, the Accusump accumulator is a cylinder with a sliding piston inside, oil on one side and pressuried air on the other. the oil side is connected to the engine's main gallery through two separate and distinct valves: a small, low flow orfice with checkvalve and a larger, electrically controlled dump valve.
The small orfice and check valve allows high-pressure engine oil to fill the accumulator relatively slowly, the piston compressing the air side until equilibrium. (Here, the accumulator has two quarts of oil at something over 70 psi, which is the cold-engine-oil startup pressure). The slow-fill assures that an empty accumulator won't starve the engine while it fills.
The second valve on the Accusump is large and electrically controlled. its purpose is to allow the pressurized oil in the accumulator to feed the engine when the oil pressure form the main pump temporarily plummets; in my typical case, in severe turns at speed in mountain roads (or panic-type stops) when enough oil has sloshed to one side or the other, allowing the oil pump to suck air. it typcically takes 2 to 10 seconds to recover from this during which oil pressure is zero. plain bearings don't like this especially under load.
Canton has different manual and electric solenoid valves, and different range pressure switches to control the electric solenoid valve. the switch closes (applying power to the solenoid, opening the valve) at a fixed pressure, and opens (powers off) at a somewhat higher fixed pressure. the trick is to pick a pressure switch that remains closed during typical idle (lowest speed/lowest normal oil pressure).
My engine idles at 600 rpm where oil pressure is typically 35 - 40 psi and i selected a switch that closes (turns on) at 35 psi and off at 40 psi. This would mean that when I throttled back the accumulator would dump oil until it equalized to idle pressure (eg. 35 psi). In my case I added a computer output that is "off" below 800 rpm and drive the switch from that. any aftermarket ignitions (eg. MegaJolt Lite Jr, Megasquirt, etc) have outputs for this. or simply set the idle up, or put up with it as-is; in my case at speed the thing would be full anyway under load/speed when I needed it.
The second thing that sold me on the Accusump is that it provides full-pressure engine pre-oiling. at ignition-on the switch is closed (0 psi), solenoid open and the accumulator pushes oil into the engine until it reaches the "off" pressure (40 psi here). takes about two seconds.
the Accusump makes oil changes slightly more complicated. before draining
the oil the accumulator must be emptied; simply power the solenoid on until the
air pressure gauge reads minimum. after draining and refilling, pull a wire off
the switch/solenoid to ensure that the big valve does not open and
starve the engine. post-oil-change is the one time when the accumulator is
empty and there is no oil in the gallery.
This oil pump is very old technology. Huge clearances, rough castings, heavy, cheap to make, and reliable. Note the rough casting in the pump outlet! There's a lot of room for improvement here...
My first modified oil pump failed.
Stock gear-end clearances on the stock pump run about .008 - .009". Hoping to improve oiling, I carefully ground the pump body down so that total gear-to-cover clearance was about .002". Oil volume and pressure went way way up -- 40+ psi at idle, 60 - 80 psi above 1500 rpm. In fact I had problems with the bypass valve not able to dump enough oil back into the pan to keep cold-engine pressures under control. 2000 miles later, the driven gear nicked the cover, and momentarily locked, shearing teeth off the drive gear. (I shut the engine down immediately, it seems no further harm done.)
At that time, 2010 or 2011, I replaced it with a factury pump, with the blocking plate and custom cover and full flow filtration. Pressures are a more normal 25+ psi at idle, 50 - 60 psi hot 1600 rpm and up. Somewhere between these two extremes, .002" excessively tight, .009" factory loose, is probably a happy compromise. Without a specific reason I'm reluctant to do the experiments. Probably dropping clearances to .005 - .006" would make for a healthy increase without any reliabity threat. (the pump needs explicit end-play control, such as a ball.)
note the pump packed with vaseline for initial startup -- this is required. it is not possible to prime the pump externally. it is geared directly to the camshaft, not via the distributor drive gear. it's a slight pain to pack but keep the gasket surface grease-free so that sealer will seal, but this is a critical feature.
The aluminum engine (used only in the 10 series (Classic) chassis) had a pump that incorporated full-flow filtration; in 1964 that pump was installed in iron 195.6 OHV engines in the new-for-1964 01 series (American). the filter on this pump will not clear the suspension or chassis of the pre-1964 01/American.
i got a rusted '64 pump from a friend, it was too far gone to use but it served as a model for cogitating on a solution. The fundamental limitation in the pre-1964 American chassis is clearance. I believe that if I had a decent Classic pump I could have modified it for my own ends, but I couldn't find one, and the non-filter pump is common enough so I based my hack on that.
Below are some pics of the 1965 full-flow filtration pump I got from Joe. Though the casting was too pitted to be used, I did make mods to it that would have solved the problem.
This casting is based upon the venerable old pump, but has a complicated cover that incorporates the overpressure bypass that dumps oil back to the pump inlet; therefore the filter will never get unregulated pressure. That's a required choice for an OEM environment, but not a much of a worry in mine.
Worse, this pump does not fit the earlier blocks; the block casting is wider at the pump mounting face, because there is a passageway in the pump outlet that requires the block face to seal it. The old blocks have air where the new block has cast iron.
However, I needed to block that outlet anyways, so I fabricated a steel button that would clamp under the pump body and block the main gallery passageway. Additionally, the pump outlet would be drilled and tapped as is the other pump. This made the button dimensions critical (note the paint marks I used to verify alignment and contact area) and in the end I abandoned this path; the other pump is far easier to mod, far more common and is in fact lower-profile than the 1965 pump.